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Thread: Epg causes logo infinite loop

  1. #1

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    Epg causes logo infinite loop

    Cable vermin epg is set up to update once a day. After few minutes vix logo comes on spinning for ages in left upper corner thus unable to change channel etc. What can this be caused by? After full factory reset, hdd initialisation nothing happens, only after downloading and loading epg. Thanks

  2. #2
    Andy_Hazza's Avatar
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    what receiver you got?

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    Quote Originally Posted by nardeeno33 View Post
    Cable vermin epg is set up to update once a day. After few minutes vix logo comes on spinning for ages in left upper corner thus unable to change channel etc. What can this be caused by? After full factory reset, hdd initialisation nothing happens, only after downloading and loading epg. Thanks
    Can you specify what settings you are using for EPG please? Also what image (Build name and number)

  4. #4

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    Miraclebox premium mini hd, apollo 62, epg settings daily update, xmltv provider cross epg vermin cable

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    abu baniaz's Avatar
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    Cant help you with that setup. Hope somene else can.

    In the mean time , have a look at this
    http://www.world-of-satellite.com/sh...off-the-stream

  6. #6

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    I'll try that thanks

  7. #7

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    Did fresh install of 70 built, initialisation of hdd and pvr epg as you said and getting spinning logo again don't know what else could it be?

  8. #8

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    Epg causes logo infinite loop

    Cable vermin epg is set up to update once a day. After few minutes vix logo comes on spinning for ages in left upper corner thus unable to change channel etc. What can this be caused by? After full factory reset, hdd initialisation nothing happens, only after downloading and loading epg. Miraclebox premium mini hd, apollo 70. Thanks

  9. #9
    Joe_90's Avatar
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    Why have you started a second thread on this? You have one with some responses here - http://www.world-of-satellite.com/sh...-infinite-loop
    GB Quad Plus, Mut@nt HD51, AX HD61, 80cm dish and Supreme Dark motor. Sony STR-DN 1060, Sony UHP-H1 Bluray, Odroid N2+ (CoreElec), Monitor Audio Bronze 5.1 speakers

  10. #10

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    Because at first I thought it is epg related so I asked in epg section, but it might be miraclebox related therefore I tried miraclebox section, or it might be image specific so I asked in image support
    Last edited by nardeeno33; 30-10-14 at 21:17.

  11. #11
    Joe_90's Avatar
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    Can you set up a debug log and post the contents here?
    GB Quad Plus, Mut@nt HD51, AX HD61, 80cm dish and Supreme Dark motor. Sony STR-DN 1060, Sony UHP-H1 Bluray, Odroid N2+ (CoreElec), Monitor Audio Bronze 5.1 speakers

  12. #12

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    What time of the day are you updating EPG?
    Are you using any other EPG sources?
    What size is your EPG DB? Menu -> Setup -> System -> EPG -> CrossEPG -> Info about database.
    Also, as fat-tony points out, a debug log could be handy with your issue here,
    Menu -> Setup -> System -> Logs -> Settings -> Enable debug logs = yes.
    Do an E2 or box restart to enable.

  13. #13
    abu baniaz's Avatar
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    Where are you saving your EPG?

  14. #14
    abu baniaz's Avatar
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    Two EPG threads merged

  15. #15

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    Code:
    [eDVBLocalTimerHandler] time update to 18:20:59
    [eDVBLocalTimerHandler] m_time_difference is 2
    [eDVBLocalTimerHandler] set Linux Time
    [EPGC] start caching events(1414952461)
    sdt update done!
    singleRead error (Connection reset by peer)
    stop streaming
    [eFilePushThreadRecorder] stopping thread.
    [eDVBRecordStreamThread] cancelling aio
    [eDVBRecordStreamThread] all done
    [eDVBRecordFileThread] waiting for aio to complete
    [eDVBRecordFileThread] wait: aio_return returned failure: Interrupted system call
    [eDVBRecordFileThread] buffer usage histogram (4 buffers of 188 kB)
    * * * 1:* * * 6
    * * * 2:* * * 9
    [eFilePushThreadRecorder] THREAD STOP
    thread joined 0
    stop streaming
    [eDVBCAService] free slot 0 demux 1 for service 1:0:1:3360:C93:3:EB0000:0:0:0:
    [eDVBCAService] free service 1:0:1:3360:C93:3:EB0000:0:0:0:
    start release channel timer
    poll: unhandled POLLERR/HUP/NVAL for fd 24(24)
    [EPGC] abort non avail schedule other reading
    [EPGC] abort non avail virgin nownext reading
    [EPGC] abort non avail virgin schedule reading
    [EPGC] abort non avail netmed schedule reading
    [EPGC] abort non avail netmed schedule other reading
    [EPGC] abort non avail FreeSat schedule_other reading
    [EPGC] abort non avail viasat reading
    [EPGC] nownext finished(1414952468)
    release cached channel (timer timeout)
    [eDVBLocalTimerHandler] remove channel 0x224f640
    [eEPGCache] remove channel 0x224f640
    [EPGC] abort caching events !!
    stop release channel timer
    close frontend 0
    [SoftcamManager] mgcamd.1.35a already running
    job Components.Task.Job name=SoftcamCheck #tasks=1 completed with [] in None
    [eDVBLocalTimerHandler] diff is -2
    [eDVBLocalTimerHandler] diff < 120 .. use Transponder Time
    [eDVBLocalTimerHandler] difference between linux time and RTC time is < 60 sec... so the transponder time looks ok
    [eDVBLocalTimerHandler] time update to 18:27:59
    [eDVBLocalTimerHandler] m_time_difference is -2
    [eDVBLocalTimerHandler] set Linux Time
    [SoftcamManager] mgcamd.1.35a already running
    job Components.Task.Job name=SoftcamCheck #tasks=1 completed with [] in None
    [SoftcamManager] mgcamd.1.35a already running
    job Components.Task.Job name=SoftcamCheck #tasks=1 completed with [] in None
    [eDVBLocalTimerHandler] diff is 0
    [eDVBLocalTimerHandler] diff < 120 .. use Transponder Time
    [eDVBLocalTimerHandler] not changed
    [NTP]: setting E2 time: 1414953880.37
    set RTC to 2014/11/02 18:44 (rtc_offset = 7200 sec.)
    [SoftcamManager] mgcamd.1.35a already running
    job Components.Task.Job name=SoftcamCheck #tasks=1 completed with [] in None
    allocate channel.. 07d9:0002
    available channel.. 0020:f020
    opening frontend 0
    (0)tune
    RotorCmd ffffffff, lastRotorCmd ffffffff
    prepare_sat System 0 Freq 11876000 Pol 0 SR 27500000 INV 2 FEC 2 orbpos 282 system 0 modulation 1 pilot 2, rolloff 0
    tuning to 1276 mhz
    OURSTATE: tuning
    allocate Channel: res 0
    [eDVBCIInterfaces] addPMTHandler 1:0:1:1840:7D9:2:11A0000:0:0:0:
    allocate demux
    [SEC] set static current limiting
    set sequence pos 3
    set sequence pos 4
    [SEC] setVoltage 2
    [SEC] sleep 200ms
    [SEC] invalidate current switch params
    [SEC] sendDiseqc: e00000(DiSEqC reset)
    [SEC] sleep 50ms
    [SEC] sendDiseqc: e00003(DiSEqC peripherial power on)
    [SEC] sleep 150ms
    [SEC] sendDiseqc: e01038fb(?)
    [SEC] sleep 50ms
    set sequence pos 3
    [SEC] setTone 1
    [SEC] sleep 10ms
    [SEC] update current switch params
    [SEC] startTuneTimeout 5000
    [SEC] setFrontend 1
    setting frontend 0
    (0)fe event: status 0, inversion off, m_tuning 1
    [SEC] sleep 500ms
    (0)fe event: status 1e, inversion off, m_tuning 2
    OURSTATE: ok
    [eDVBLocalTimerHandler] channel 0x22a6b10 running
    [eEPGCache] channel 0x22a6b10 running
    [EPGC] next update in 2 sec
    stop release channel timer
    ok ... now we start!!
    STREAM service event 6
    tuned..
    PATready
    use pmtpid 0114 for service_id 1840
    STREAM service event 5
    start streaming...
    STREAM: have 1 video stream(s) (091d), and 2 audio stream(s) (091e, 091f) (0920), and the pcr pid is 091d, and the text pid is 0920
    ADD PID: 0000
    ADD PID: 0012
    ADD PID: 0014
    ADD PID: 0114
    ADD PID: 091d
    ADD PID: 091e
    ADD PID: 091f
    ADD PID: 0920
    setIoPrio realtime level 7 ok
    [eFilePushThreadRecorder] THREAD START
    [eDVBCAService] new service 1:0:1:1840:7D9:2:11A0000:0:0:0:
    [eDVBCAService] add demux 1 to slot 0 service 1:0:1:1840:7D9:2:11A0000:0:0:0:
    [eDVBCIInterfaces] gotPMT
    [SEC] set dynamic current limiting
    sdt update done!
    [EPGC] start caching events(1414953902)
    [eFilePushThreadRecorder] Warning: All write buffers busy
    [eDVBRecordFileThread] cancelling
    [eDVBRecordStreamThread] failed to cancel, killing all waiting IO
    [eDVBRecordFileThread] poll: aio_return returned failure: Interrupted system call
    [eDVBRecordFileThread] poll: aio_return returned failure: Interrupted system call
    [eDVBRecordFileThread] poll: aio_return returned failure: Interrupted system call
    [eDVBRecordFileThread] Waiting for I/O to complete
    [eDVBLocalTimerHandler] diff is 1
    [eDVBLocalTimerHandler] diff < 120 .. use Transponder Time
    [eDVBLocalTimerHandler] set RTC Time
    [eDVBLocalTimerHandler] update RTC
    [eDVBLocalTimerHandler] time update to 18:45:10
    [eDVBLocalTimerHandler] m_time_difference is 1
    [eDVBLocalTimerHandler] set Linux Time
    [EPGC] abort non avail schedule reading
    [EPGC] abort non avail schedule other reading
    [EPGC] abort non avail virgin nownext reading
    [EPGC] abort non avail virgin schedule reading
    [EPGC] abort non avail netmed schedule reading
    [EPGC] abort non avail netmed schedule other reading
    [EPGC] abort non avail FreeSat schedule_other reading
    [EPGC] abort non avail viasat reading
    [EPGC] nownext finished(1414953910)
    [EPGC] stop caching events(1414953910)
    [EPGC] next update in 60 min
    [eFilePushThreadRecorder] Warning: All write buffers busy
    [eDVBRecordFileThread] cancelling
    [eDVBRecordStreamThread] failed to cancel, killing all waiting IO
    [eDVBRecordFileThread] poll: aio_return returned failure: Interrupted system call
    [eDVBRecordFileThread] poll: aio_return returned failure: Interrupted system call
    [eDVBRecordFileThread] poll: aio_return returned failure: Interrupted system call
    [eDVBRecordFileThread] Waiting for I/O to complete
    [eFilePushThreadRecorder] Warning: All write buffers busy
    [eDVBRecordFileThread] cancelling
    [eDVBRecordStreamThread] failed to cancel, killing all waiting IO
    [eDVBRecordFileThread] poll: aio_return returned failure: Interrupted system call
    [eDVBRecordFileThread] poll: aio_return returned failure: Interrupted system call
    [eDVBRecordFileThread] poll: aio_return returned failure: Interrupted system call
    [eDVBRecordFileThread] Waiting for I/O to complete
    [eFilePushThreadRecorder] Warning: All write buffers busy
    [eDVBRecordFileThread] cancelling
    [eDVBRecordStreamThread] failed to cancel, killing all waiting IO
    [eDVBRecordFileThread] poll: aio_return returned failure: Interrupted system call
    [eDVBRecordFileThread] poll: aio_return returned failure: Interrupted system call
    [eDVBRecordFileThread] poll: aio_return returned failure: Interrupted system call
    [eDVBRecordFileThread] Waiting for I/O to complete
    stop streaming
    [eDVBRecordFileThread] poll: aio_return returned failure: Interrupted system call
    [eFilePushThreadRecorder] WRITE ERROR, aborting thread
    [eDVBRecordStreamThread] cancelling aio
    [eDVBRecordStreamThread] all done
    [eDVBRecordFileThread] waiting for aio to complete
    [eDVBRecordFileThread] wait: aio_return returned failure: Interrupted system call
    [eDVBRecordFileThread] wait: aio_return returned failure: Interrupted system call
    [eDVBRecordFileThread] buffer usage histogram (4 buffers of 188 kB)
    * * * 0:* * * 1
    * * * 1:* * *16
    * * * 2:* * *14
    * * * 3:* * *40
    * * * 4:* * * 4
    [eFilePushThreadRecorder] THREAD STOP
    [eFilePushThreadRecorder] stopping thread.
    send signal to non running thread
    thread joined 0
    stop streaming
    [eDVBCAService] free slot 0 demux 1 for service 1:0:1:1840:7D9:2:11A0000:0:0:0:
    [eDVBCAService] free service 1:0:1:1840:7D9:2:11A0000:0:0:0:
    start release channel timer
    poll: unhandled POLLERR/HUP/NVAL for fd 24(24)
    release cached channel (timer timeout)
    [eDVBLocalTimerHandler] remove channel 0x22a6b10
    [eEPGCache] remove channel 0x22a6b10
    stop release channel timer
    close frontend 0
    allocate channel.. 07d9:0002
    available channel.. 0020:f020
    opening frontend 0
    (0)tune
    RotorCmd ffffffff, lastRotorCmd ffffffff
    prepare_sat System 0 Freq 11876000 Pol 0 SR 27500000 INV 2 FEC 2 orbpos 282 system 0 modulation 1 pilot 2, rolloff 0
    tuning to 1276 mhz
    OURSTATE: tuning
    allocate Channel: res 0
    [eDVBCIInterfaces] addPMTHandler 1:0:1:1840:7D9:2:11A0000:0:0:0:
    allocate demux
    [SEC] set static current limiting
    set sequence pos 3
    set sequence pos 4
    [SEC] setVoltage 2
    [SEC] sleep 200ms
    [SEC] invalidate current switch params
    [SEC] sendDiseqc: e00000(DiSEqC reset)
    [SEC] sleep 50ms
    [SEC] sendDiseqc: e00003(DiSEqC peripherial power on)
    [SEC] sleep 150ms
    [SEC] sendDiseqc: e01038fb(?)
    [SEC] sleep 50ms
    set sequence pos 3
    [SEC] setTone 1
    [SEC] sleep 10ms
    [SEC] update current switch params
    [SEC] startTuneTimeout 5000
    [SEC] setFrontend 1
    setting frontend 0
    (0)fe event: status 0, inversion off, m_tuning 1
    [SEC] sleep 500ms
    (0)fe event: status 1e, inversion off, m_tuning 2
    OURSTATE: ok
    [eDVBLocalTimerHandler] channel 0x22a6850 running
    [eEPGCache] channel 0x22a6850 running
    [EPGC] next update in 59 min
    stop release channel timer
    ok ... now we start!!
    STREAM service event 6
    tuned..
    PATready
    use pmtpid 0114 for service_id 1840
    [eDVBLocalTimerHandler] diff is 0
    [eDVBLocalTimerHandler] diff < 120 .. use Transponder Time
    [eDVBLocalTimerHandler] not changed
    STREAM service event 5
    start streaming...
    STREAM: have 1 video stream(s) (091d), and 2 audio stream(s) (091e, 091f) (0920), and the pcr pid is 091d, and the text pid is 0920
    ADD PID: 0000
    ADD PID: 0012
    ADD PID: 0014
    ADD PID: 0114
    ADD PID: 091d
    ADD PID: 091e
    ADD PID: 091f
    ADD PID: 0920
    setIoPrio realtime level 7 ok
    [eFilePushThreadRecorder] THREAD START
    [eDVBCAService] new service 1:0:1:1840:7D9:2:11A0000:0:0:0:
    [eDVBCAService] add demux 1 to slot 0 service 1:0:1:1840:7D9:2:11A0000:0:0:0:
    [eDVBCIInterfaces] gotPMT
    [eDVBCAService] don't build/send the same CA PMT twice
    [SEC] set dynamic current limiting
    sdt update done!
    stop streaming
    [eFilePushThreadRecorder] stopping thread.
    [eFilePushThreadRecorder] *read error* (Bad file descriptor) - aborting thread because i don't know what else to do.
    [eDVBRecordStreamThread] cancelling aio
    [eDVBRecordStreamThread] not all cancelled
    [eDVBRecordFileThread] waiting for aio to complete
    [eDVBRecordFileThread] Waiting for I/O to complete
    main thread is non-idle! display spinner!
    [eDVBRecordFileThread] wait: aio_return returned failure: Bad file descriptor
    [eDVBRecordFileThread] wait: aio_return returned failure: Bad file descriptor
    [eDVBRecordFileThread] buffer usage histogram (4 buffers of 188 kB)
    * * * 1:* * * 1
    * * * 2:* * * 4
    * * * 3:* * * 3
    [eFilePushThreadRecorder] THREAD STOP
    thread joined 0
    stop streaming
    [eDVBCAService] free slot 0 demux 1 for service 1:0:1:1840:7D9:2:11A0000:0:0:0:
    [eDVBCAService] free service 1:0:1:1840:7D9:2:11A0000:0:0:0:
    start release channel timer
    [AutoTimer] Auto Poll
    [AutoTimer] Auto Poll Started
    [AutoTimer] No changes in configuration, won't parse
    job Components.Task.Job name=AutoTimer #tasks=0 completed with [] in None
    [SoftcamManager] mgcamd.1.35a already running
    [eDVBLocalTimerHandler] diff is -5
    [eDVBLocalTimerHandler] diff < 120 .. use Transponder Time
    [eDVBLocalTimerHandler] difference between linux time and RTC time is < 60 sec... so the transponder time looks ok
    [eDVBLocalTimerHandler] time update to 19:02:21
    [eDVBLocalTimerHandler] m_time_difference is -5
    [eDVBLocalTimerHandler] set Linux Time
    ERROR reading PES (fd=61) - Value too large for defined data type
    poll: unhandled POLLERR/HUP/NVAL for fd 61(8)
    job Components.Task.Job name=SoftcamCheck #tasks=1 completed with [] in None
    release cached channel (timer timeout)
    [eDVBLocalTimerHandler] remove channel 0x22a6850
    [eEPGCache] remove channel 0x22a6850
    stop release channel timer
    allocate channel.. 07ec:0002
    available channel.. 0020:f020
    (0)tune
    RotorCmd ffffffff, lastRotorCmd ffffffff
    prepare_sat System 1 Freq 12246000 Pol 1 SR 29500000 INV 2 FEC 3 orbpos 282 system 1 modulation 1 pilot 2, rolloff 1
    tuning to 1646 mhz
    OURSTATE: tuning
    allocate Channel: res 0
    [eDVBCIInterfaces] addPMTHandler 1:0:19:EE6:7EC:2:11A0000:0:0:0:
    allocate demux
    [SEC] set static current limiting
    stop streaming
    stop streaming
    start release channel timer
    [SEC] setTone 0
    [SEC] sleep 25ms
    [SEC] setVoltage 1
    [SEC] sleep 20ms
    set sequence pos 3
    [SEC] invalidate current switch params
    [SEC] sendDiseqc: e01038f9(?)
    [SEC] sleep 50ms
    set sequence pos 3
    [SEC] setTone 1
    [SEC] sleep 10ms
    [SEC] update current switch params
    [SEC] startTuneTimeout 5000
    [SEC] setFrontend 1
    setting frontend 0
    (0)fe event: status 0, inversion off, m_tuning 1
    [SEC] sleep 500ms
    (0)fe event: status 1e, inversion off, m_tuning 2
    OURSTATE: ok
    [eDVBLocalTimerHandler] channel 0x229d050 running
    [eEPGCache] channel 0x229d050 running
    [EPGC] next update in 2 sec
    stop release channel timer
    [SEC] set dynamic current limiting
    [EPGC] start caching events(1414954944)
    [eDVBLocalTimerHandler] diff is 5
    [eDVBLocalTimerHandler] diff < 120 .. use Transponder Time
    [eDVBLocalTimerHandler] set RTC Time
    [eDVBLocalTimerHandler] update RTC
    [eDVBLocalTimerHandler] time update to 19:02:30
    [eDVBLocalTimerHandler] m_time_difference is 5
    [eDVBLocalTimerHandler] set Linux Time
    [EPGC] abort non avail schedule reading
    [EPGC] abort non avail schedule other reading
    [EPGC] abort non avail virgin nownext reading
    [EPGC] abort non avail virgin schedule reading
    [EPGC] abort non avail netmed schedule reading
    [EPGC] abort non avail netmed schedule other reading
    [EPGC] abort non avail FreeSat schedule_other reading
    [EPGC] abort non avail viasat reading
    [EPGC] nownext finished(1414954956)
    [EPGC] stop caching events(1414954956)
    [EPGC] next update in 60 min
    [SoftcamManager] mgcamd.1.35a already running
    job Components.Task.Job name=SoftcamCheck #tasks=1 completed with [] in None
    [SoftcamManager] mgcamd.1.35a already running
    job Components.Task.Job name=SoftcamCheck #tasks=1 completed with [] in None
    [LogManager] Trim Poll Started
    job Components.Task.Job name=LogManager #tasks=1 completed with [] in None
    [NTP]: setting E2 time: 1414955681.43
    set RTC to 2014/11/02 19:14 (rtc_offset = 7200 sec.)
    [MetrixWeather] lookup for ID 640161
    KEY: 139 MENU
    action ->* InfobarMenuActions mainMenu
    KEY: 139 MENU
    KEY: 103 UP
    KEY: 103 UP
    KEY: 103 UP
    KEY: 103 UP
    KEY: 352 OK
    action ->* OkCancelActions ok
    KEY: 352 OK
    KEY: 103 UP
    KEY: 103 UP
    KEY: 108 DOWN
    KEY: 108 DOWN
    KEY: 352 OK
    action ->* OkCancelActions ok
    KEY: 352 OK
    KEY: 103 UP
    KEY: 103 UP
    KEY: 103 UP
    KEY: 103 UP
    KEY: 103 UP
    KEY: 103 UP
    KEY: 103 UP
    KEY: 103 UP
    KEY: 103 UP
    KEY: 103 UP
    KEY: 103 UP
    KEY: 103 UP
    KEY: 103 UP
    KEY: 103 UP
    KEY: 103 UP
    KEY: 103 UP
    KEY: 103 UP
    KEY: 103 UP
    KEY: 352 OK
    action ->* OkCancelActions ok
    KEY: 352 OK
    KEY: 108 DOWN
    KEY: 108 DOWN
    KEY: 352 OK
    action ->* OkCancelActions ok
    warning, skin is missing element LogsSize in <class 'Screens.LogManager.LogManager'>
    KEY: 352 OK
    KEY: 398 RED
    KEY: 398 RED
    action ->* ColorActions red
    KEY: 398 RED
    KEY: 398 RED
    action ->* ColorActions red
    KEY: 398 RED
    KEY: 398 RED
    action ->* ColorActions red
    KEY: 401 BLUE
    KEY: 401 BLUE
    action ->* ColorActions blue
    KEY: 352 OK
    action ->* MsgBoxActions ok
    KEY: 352 OK
    KEY: 108 DOWN
    action ->* DirectionActions down
    KEY: 108 DOWN
    KEY: 352 OK
    action ->* MsgBoxActions ok
    KEY: 352 OK
    Last edited by abu baniaz; 02-11-14 at 21:47. Reason: code

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